Written by martin on June 23rd, 2007 12:43 pm
This review has been a few weeks coming as we have all been rather busy, but as anyone who attended the meeting will know there was not a huge amount to report on save an awful lot of rain.
Friday was largely dry and saw sportsman classes run through a huge number of qualifying cycles, which should have been good for us. However on warming the car up on Friday morning we discovered an oiling problem in one of the cylinders, which was hugely smokey, We had no option but to take the head off at this point with visions of holed pistons racing through our minds. With the head off the piston and valves were thankfully absolutely fine but it was obvious that we had head sealing problems which were traced to stripped threads in the block. It is a good thing indeed that we had the head off as running like this may have lead to torched heads.
As a precautionary measure we checked both heads and eventually fixed quite a few head studs with helicoils, checking valve seats and guides while we had the opportunity. By the time we had got the engine back together racing was done for the day, and after chasing some gremlins in the timing system the motor sounded great. We eagerly awaited Saturday to try it out.
Saturday came, and we still had a slightly oil cylinder on one sidde which we have put down to the oil control ring. We warmed the motor up and it sounded great, but on the track the performance was a bit lacklustre. Back in the pits we fired the motor and it sounded awful - checking the timing showed it was now severely retarded. We re-timed the mag and tried again, it was a bit better but not much. Back in the pits again it was obvious the mag is moving at the hit of the throttle - possibly even in the burnout - and throwing the timing out. Unfortunately this was the last run of the weekend, Sunday saw us do nothing ore than eat Roast Beef and watch Hot Rod in the back of the lorry and come Monday morning we packed up and went home, despite having qualified on the ladder. This turned out to be good call as the meeting was later called off.
We sat out the Summer Nationals as we had not received the parts required, and the motor is now being freshened for the Nostalgia Nationals with new rings and a beefier mag clamp. this should hopefully see Iron Dan perform to his full potential.
Videos from the Main Event are now online: Qualifier 1, Qualifier 2.
Written by martin on April 17th, 2007 1:08 pm
The Easter Thunderball saw an exciting event for Time Machine Racing - our new Big Block Chevy was christened ‘Iron Dan’ - now if anyone asks if you know Dan you can say you do.
Dan was not the happiest of engines at Easter though, seemingly grumpy at being woke from his hibernation so early in the year. I can’t see what he was complaining about though as the weather was some of the balmiest I have seen at Easter - rather than the normal snow there was sunshine and lots of it, even featuring shorts and t-shirts on one day.
We spent a while chasing down a problem in the fuel system only to find that when we thought we had sorted it the motor was running really hot and seemingly lean. A quick sanity check showed this to actually be caused by the mag clamp coming loose and allowing the timing to retard itself, shooting the spark while the exhaust valve is open and causing lots of flame.
This was a quick fix, but on attempting to fire the car we discovered two things - our starter motor is really getting worn out, and we had broken a bearing in the gearbox, putting us out of action.
Despite this we had a good weekend, and the event looks like going down in history as a classic. Congratulations to those running new personal bests, especially Frank Bennett and Joe Bond, and many many thanks to those who provided us with help all weekend, especially Martyn Jones and Crunch who made us feel very welcome in the Super Pro pits - I am already looking forward to the Main Event, our next scheduled appearance.
Written by martin on March 9th, 2007 1:09 pm
In 4 weeks time it will be Easter. Scary isn’t it? This year should see us competing a full season in Super Pro and we are very much looking forward to it. We may have a few surprises for you this year too - not only have we been rebuilding the engine after finding a broken lifter but we have been making a few subtle cosmetic changes to the car.
It isn’t just the car on the mend either - Darren is getting better after his recent stay in hospital.
More news soon, and see you at the track.
Written by martin on January 22nd, 2007 1:10 pm
Here at Time Machine Racing we would all like to say a huge get well soon to our crew chief Darren Galloway, who is in hospital following a triple heart attack last week.
We wouldn’t be racing now if it wasn’t for all Darren’s hard work over the years, and wish him a speedy recovery. He was last seen hassling the nurses for more ‘Nitrolingual’ as we all know that the more nitro you can get the better.
If you would like to talk to Darren then his bedside number is 07041 136273.
Written by adam on November 8th, 2006 1:10 pm
Last race meeting of the year and my second with the car, after the rain at the National Finals we woke up to the Sun (all be it cold!) on Saturday morning with the car ready to go after Darren re-did the plug leads Friday night.
Now with full throttle I was the first car down the track, pulled a nice strong burnout but at the hit it smoked the tyres and the back end stepped out so I gave it a quick pedal and pulled second which straightened it out nice, I ran through to the 1/8th and clicked off.
The second pass was much more successful, the car hooked up hard running a 1.36 60ft and 6.13@108mph at the half track mark but as I didn’t feel it go into third I shutoff coasting through with a 10.83. Upon inspection in the pits we had a trans leak (fortunately the trans blanket held most of it from going on the track).
The leak sorted I went round to do my final licensing pass but as it transpired we broke a pushrod (on the burnout we think) and the run was only on seven cylinders, the car felt very loose so I lifted a few times around half track and ran through with an 11@120mph, not quick enough for my Super Pro license but that will come next year.
The car is now at Doug Ripley’s for a winter diet and a few bits of work. We’ve got a few cosmetic changes planned for the off-season too including the full paint.
Quick thanks to the crew for their help again and to everyone who stopped by to say hello and wished us well.
Roll on 2007!